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  1. #11
    ColorGOD
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    Check the drive gear on M18. They are plastic and if the toner tube got clogged at some point the gears might have stripped. Even if they look good they might be jumping. This will cause the toner to evacuate much slower and cause another backup.

  2. #12
    Senior Tech 100+ Posts excanonguy's Avatar
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    Quote Originally Posted by ColorGOD View Post
    Check the drive gear on M18. They are plastic and if the toner tube got clogged at some point the gears might have stripped. Even if they look good they might be jumping. This will cause the toner to evacuate much slower and cause another backup.
    I was just wondering what the resolution for this problem ended up being?? I have one doing the same thing now.

  3. #13
    Senior Tech 100+ Posts excanonguy's Avatar
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    Back to the top

  4. #14
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    I have a similar problem. How did you resolve this issue. please help

  5. #15
    All things Konica Minolta 1,000+ Posts Stirton.M's Avatar
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    Description
    F23-10/SC23-10.
    Solution
    PROBABLE CAUSES:
    1.The first transfer roller sensor (PS15) is detecting a malfunction in timing between the sensor and the transfer pressing/releasing motor (M19).
    Check that all 4 transfer rollers (p/n 65AA26040 - Black, p/n 65AA26120 - colors) inside the transfer belt are seated properly in there respective front and rear
    block holder assembles. Check the operation of M19 in the 47 mode, multimode 48, code 0, 2, and 3. Check PS15 in the 47 mode, multimode 48, code 0, 1,
    2, and 3, for home position = 01; other than home position = 000.
    2. The position of M19 is determined by PS15. If PS15 is out of place or faulty, M19 cannot find home position.
    Note : When activated in 47 mode, M19 does not stop rotating.
    Inspect PS15 (p/n 08AA 8551 2) and replace it if necessary.
    "Many years ago I chased a woman for almost two years, only to discover that her tastes were exactly like mine: we both were crazy about girls."
    ---Groucho Marx


    Please do not PM me for questions related to Konica Minolta hardware.
    I will not answer requests or questions there.
    Please ask in the KM forum for the benefit of others to see the question and give their input.

  6. #16
    All things Konica Minolta 1,000+ Posts Stirton.M's Avatar
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    Description
    F23-09 with lines, smudges or spots on copies.
    Solution
    PROBABLE CAUSES:
    1. Insufficient airflow during idle causing internal machine temperature to rise. Toner is backing up or solidifying in the cleaning unit box for the transfer belt
    causing the transfer belt drive motor (M18) to bind.
    Replace the Belt Cleaning Unit (p/n 65LA R702 00) and install attachedSpecial Printer Control firmware(version 51-PBF0 for the 8050/CF5001 and version
    12-PBF0 for the bizhub PRO C500 ).This firmwarekeeps M11 (Transfer Belt Cooling Fan) ON for a period after the copy process has completed which helps
    keep the internal temperature at normal levels. The firmware can also be download from the Konica Minolta Download Selector. Access the Selector from
    SSD Web Support (CS Expert Support) by clicking on 'Download MSDS, Drivers, Firmware and more'.
    Note : Firmware version 51-PBF0 is primarily for the 8050, but can be usedfor the CF5001. When using the ISW tool to download the firmware please
    select the 8050 from the drop down. If the CF5001 is selectedthe ISW tool will not see the file.
    2. The paper exit fans (M61/M62/M63) DIPswitch is not turned ON.
    Set software DIPSW 21-0 = 1 to enable the paper exit fans.
    3. Dirty or failed transfer belt drive motor encoder disk sensor assembly.
    Clean the transfer belt drive motor encoder disk and sensors. Replace the assembly (p/n 65AA -909 1E) as necessary.
    4. Failed M18 transfer belt drive motor.
    Replace M18 transfer belt drive motor (p/n 26WA 8001 3).
    "Many years ago I chased a woman for almost two years, only to discover that her tastes were exactly like mine: we both were crazy about girls."
    ---Groucho Marx


    Please do not PM me for questions related to Konica Minolta hardware.
    I will not answer requests or questions there.
    Please ask in the KM forum for the benefit of others to see the question and give their input.

  7. #17
    Technician
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    Re: C500 Error Code 23-09

    Same problem here. Did all of the tests. Replaced the Printer control board, Transfer belt cleaning unit, swapped the transfer belt motor and sensors from another C500 that booted with the problem. Cleaned the waster toner auger. Checked the firmware and it is current, Dip switch is set to allow extended airflow etc. Have noticed that the motor spins intermittently when run in 47 mode 41 multi-mode 11,12,13. What could cause this motor not to spin. Bear in mind that the current one is from a C500 that boots without this error. Need some advice tofix this C500.

  8. #18
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    Re: C500 Error Code 23-09

    Was hoping someone can chime in with an update. Did not want to start a new thread as everything described here is exactly how this machine is behaving. We are stuck. Have we missed something. The motor is fine as it is working in a another C500. The transfer belt seems OK. New transfer belt cleaning unit installed. The transfer belt roller are seated properly. New Printer control Board installed. The Waste Toner pipes cleaned. What else should we be looking for. What have me missed. Interestingly the motor does not spin in 47 mode - 41 multi-mode 11, 12 & 13. What could cause that? Really looking for some help here.

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